I Sherlock'd My Dead Big Block Chevy and Found Out Why It Broke!
Summary
TLDRThe video details the process of diagnosing issues with a 632 cubic inch big block Chevy drag boat engine that failed during racing. After tearing down the engine and inspecting the parts, evidence of metal-to-metal contact between the exhaust valves and pistons is discovered, likely causing bearing failure. Measurements confirm lack of proper piston to valve clearance. The engine issues stem from a rushed rebuild prior to competition where clearances were not properly checked. The rebuild compromised power, reliability and ultimately caused catastrophic failure. While rebuilding again is possible, a different engine will likely go into the boat for the next race season.
Takeaways
- 😟 The 632 cubic inch big block Chevy engine broke at a drag boat race event last year, so Cleetus is finally tearing it down to diagnose the failure
- 😞 There were ongoing valve train issues with the heads that were never fully resolved, likely causing component failures
- 🤔 The crank, rods, and pistons were replaced when converting the engine for nitrous, but clearances seem to be incorrect
- 😟 Bearing damage indicates debris circulated through the engine, wearing down components prematurely
- 😟 Evidence suggests exhaust valves were contacting the pistons, damaging both
- 😔 All of the exhaust valves are bent from contact with pistons and guides are damaged
- ☹️ The lightweight NA parts were never meant for the rigors of nitrous and are now compromised
- 😕 Proper clearances are critical, the installed parts had insufficient piston to valve clearance
- 😐 The engine builder is talented but time pressures led to overlooked measurements
- 🙂 Despite engine issues, Cleetus still had fun racing with friends and learned a lot diagnosing failures
Q & A
What type of engine is being worked on in the video?
-A 632 cubic inch big block Chevy engine.
What happened to the engine that caused it to break at the drag boat race?
-The engine dropped a valve which caused it to lock up and break.
What mods were done to the engine to prepare it for nitrous?
-It got a new crank, rods, and pistons.
What issue was discovered when disassembling the engine?
-There was evidence of the exhaust valves contacting the pistons due to insufficient piston to valve clearance.
How did the lack of piston to valve clearance manifest itself?
-There were circular wear marks on the pistons that matched marks on the exhaust valves.
What other issues were found with the engine?
-The crankshaft bearings showed uneven wear indicating a possible issue with the crank flexing or taper in the journals.
What will need to be replaced to fix the engine?
-The valves, pistons, and possibly the crank will need replacement. The cylinder heads may also need work.
Why did the engine builder miss the clearance issue originally?
-He was in a hurry and didn't have time to check all the clearances before assembly.
What was done to measure the existing piston to valve clearance?
-The engine was reassembled with lightweight checking springs and the clearances were measured with a dial indicator.
What engine will go in the boat next instead of rebuilding this one?
-A proven reliable engine built by Sonny already sitting in the boat will likely be used next.
Outlines
😀 Preliminary inspection of the broken engine
The video host inspects the disassembled 632 cubic inch big block Chevy drag boat engine that broke at a race last year. He expresses excitement to rebuild it, noting the corrosion damage from water exposure at the race track.
🌊 The engine's racing history and previous issues
The host outlines the engine's past - originally built by Jim Guthy, raced successfully by Joola Camp to a championship win, then sold to the current owner. It has had recurring issues like broken valves and leaking cylinder heads that have been repaired multiple times.
🔧 Preparing to disassemble and inspect the engine
To diagnose the recurring issues, the host begins disassembling the engine by removing accessories like the tunnel ram intake manifold. He points out grounding issues with the nitrous system wiring and improper head bolt torque procedures.
🤔 Assessing damage from the last failure
With the heads removed, the host finds significant damage from the last failure including bent valves, damaged guides, debris in the cylinders. He suspects incorrectly reassembled rocker arms caused valvetrain issues.
🔬 Inspecting the bottom end parts
The host removes the oil pan, crankshaft, pistons and connecting rods to inspect the bottom end components. He finds some detonation damage and improperly gapped piston rings among other issues.
🚣 Measuring crankshaft journals to check for taper
Using a micrometer, the host carefully measures the crankshaft main and rod journals at different points to check for taper. Finding none, he rules out the crank flexing as the cause of the bearing damage.
💡 Discovering evidence of piston-to-valve contact
Noticing odd wear marks on the pistons matching those on the valves, the host determines that inadequate piston-to-valve clearance led to contact between the exhaust valves and pistons.
🤯 Explaining the piston skirt dents
The host further discovers multiple pistons have dented skirts from hitting the crank counterweights during assembly. This caused even tighter clearances and more valvetrain issues.
🔍 Investigating piston deck height
They measure how far the piston is protruding from the cylinder bore and use check springs to manually activate the valves and physically check piston-to-valve clearances.
😔 Bent valves confirm the diagnosis
Putting the valves in a lathe, the host finds they are significantly bent, confirming intermittent contact with the pistons led to the failures. Major repairs are required before the engine can race again.
Mindmap
Keywords
💡engine
💡bearings
💡detonation
💡pistons
💡valves
💡clearance
💡rebuild
💡crankshaft
💡damage
💡diagnosis
Highlights
The motor locked up at the drag racing finals last year, so it's finally being torn down to diagnose the failure
The crank, rods, and pistons were recently changed to run nitrous, but it ended up slower and unreliable
Found evidence of the exhaust valves repeatedly hitting the pistons, causing damage
Swirl marks on the pistons match machine marks on the exhaust valves
The exhaust valve guides are damaged from the valves bending when hitting pistons
Going to measure the actual piston to valve clearance to understand what's enough
Putting in lightweight "checker" valve springs so the valves can be manually operated
At 10 degrees before TDC, the exhaust valve is still closing as the piston comes up
Measured only 0.125" piston to exhaust valve clearance, seems tight given the damage
The intake valves likely were also hitting pistons, based on marks in those areas
Took the valves out and put them in a lathe - confirmed they are bent from hitting pistons
The valve train may have lacked control, letting valves bounce into pistons at high RPM
Will be repairing with increased piston to valve clearances to prevent future failure
For now, will run a spare motor instead of rebuilding this one due to the extensive repairs needed
Hope the engine builder doesn't get upset, this is meant as an educational breakdown of what went wrong
Transcripts
it took two days of measuring parts for
this 632 cubic inch big block Chevy but
I finally know why this thing broke at
the World Finals of dragboat racing last
year and right about now this big block
Chevy is making the Hemi and that b air
looked damn nice and
reliable that still runs this uh not so
much and I don't know if I'm fixing it
anytime soon watch
[Applause]
this
[Applause]
[Music]
I don't know why I'm so excited to see a
motor that I know is broken I know why
cuz I was at Ace Racing Engines two days
ago measuring bearing clearances on an
LS motor and I forgot how much fun it
was to build Motors we're going to work
on this one
ourselves if my skills with a drill are
any indication yeah you're you turn
wrenches and not not building a
house shout out to Andy RS at RS
precision machine for cading up the 632
big block Chevy we broke World Finals
after uh I believe I said it was five
passes it broke I think it was six well
this will be interesting because I
bought the boat complete and the motor
was fresh when I bought it but I didn't
know exactly what parts were in it I had
the motor rebuilt these are the parts
that came out of it so now we get to
find out you know what was in it to
begin with these parts were all set up
for this motor to be naturally aspirated
so they're lighter stuff yeah look how
corroded everything is from being in
Firebird which is the equivalent of
saltwater Wild Horse Pass that track
used to be called Firebird so we all
still call it firebird and it just
corrodes everything anything that gets
wet Firebird again though oh yeah they
changed the name again didn't they yep
back to Firebird back to
firebird and this is the original tunnel
ram off that motor that engine loved
this tunnel ram with these long Runners
and it did not like this tunnel ram with
these shorter Runners and I'm sure there
was a way to tune around that but this
thing was down like 500 RPM at wide open
throttle all that changed were piston
rods and crank same displacement little
less compression it was down over 100
horsepower so something was unhappy
about
it like brand new not even not even
scuffed let's see if we can figure out
what kind of Crank out of this thing
4750 racing crank the rest of it's gone
that's the stroke you can see where it
had a lot of malerie shoved into it to
balance it so whoevers it was gone I
wonder if it's a Bryant it's had a ton
of work to it look how thin the
counterweights are and look how long
they are because of how big the stroke
is this is the 632 combo is an
interesting combo it's 4 and 3/4 stroke
and I believe it's 4600 bore and I don't
know I'm not a huge fan of that
particular combo however when this was
actually aspirated that boat ran really
well all right we don't know what it is
but it's a damn nice looking crank
that's a beautiful crank and I believe
this stuff should be CP pistons and
cillo connecting rocks I'm almost
positive Brian Morland designed these
way back in the day for DOA camp and
this is what was put in this
motor and I think what we're going to
see if these are them is short
compression
height wrist pin up in the oil ring like
real thin Pro Stock looking oh yeah look
at that look how short this piston is
wow look at that the oil ring it's got a
support rail cuz it's the wrist pin is
up into the oil ring look how small the
wrist pin is I was just going to say
that is a small wrist pin this is one of
the reasons we couldn't put nitrous to
this thing first off there's not much
meat between the top of the Piston
especially in the valve relief area so
there's the exhaust valve relief this is
the intake valve relief there's not much
material between the top ring and that
so that's no good for nitrous then the
wrist pin is really small and light if
you threw nitrous at this it's going to
flex these rods are also really light
like if you look at how deep this
channel is yeah that channel there that
channel there the meat of that Rod is
probably a/ inch wide this is
lightweight naturally aspirated Go Fast
Pro Stock looking stuff so that means if
that thing didn't get honed where it had
a ton of piss in the wall clearance with
this this could go back together na it
would be a drag deal it used to make
like allegedly 1250 horsepower Na and uh
and it ran good when it wasn't breaking
valve springs that's the other thing is
I would love to know why did it have so
many valve train
problems so then the next thing to do is
uh pull the intake and the carbs off
pull the heads off and find out did it
screw up a piston that'll be an
interesting thing because it ran crappy
all weekend it was not fast right but
the night before it broke when I was in
the pits we checked the valve springs we
checked the valve lash the push rods
were all in one piece it wasn't broken
it just didn't run good and then I made
a hit sounded fine just wasn't fast
drove it off the lake put it on the
trailer drove it into the pits and we
started doing a compression check
and that's when the motor locked up and
so it had no compression we were about
to pull the valve cover and I hit the
button a few more times and then the
motor locked up so the push rod broke
somewhere driving it to the ramp I guess
and then the valve broke when we were
rolling it over so maybe we get lucky
the one thing that tells me we might we
might not get lucky is I've had another
motor it was actually blast me we had
something on top of the piston in the
cylinder just hit the start button and
it went went up there and pinched it and
it was enough to Dent the Piston Dent
the valve seat basically the head had to
come off and get welded it's possible
that piston and that head and you work
but I don't know we'll take it apart and
find out this is what happens in a
working garage with you know leaves
blowing in when the doors open and so
now we got that off the floor we'll blow
it out then we'll take motor carburetor
off these are gen 3 Holly dominators
that have had a good bit of work done to
them by John Morland at C&J engineering
that's why they're not for sale cuz John
is in my opinion one of the best carb
guys on the planet I hope he never
retires it do it down don't wor it
didn't go inside coming apart but I'd
still like to not not drop things in the
M possible unfortunately these are
stainless washers I can't use a magnet
to get them off I got to lift it and
hopefully not drop them peek down you
can see the plenum
bars yeah that's the second stage of
nitrous that we never hit never used it
thank God I think we would have been in
a lot more trouble
yeah yeah the first stage didn't work
great the second stage would have
probably not made it better no we can uh
disconnect Nitrous system and fuel
regulators and then unbolt the tunnel
ram and get the tunnel ram off we're
taking off the manifold bolts which are
a really nice ARP stainless 12 point um
and we're taking note of how the bolts
are now this bolt really tight this one
that had the ground wires going to the
nitrous solenoids snug but not tight and
one of the things I don't like I was
talking about I don't like it when
people ground nitrenoids or ignition
coils to bolts in the intake manifold or
the valve cover because that bolt goes
into the valley right that bolt has
thread sealant on it because it's going
into the valley it's not a blind bolt so
now you're just relying on the ring
terminal up against the washer and the
flange of the intake for a ground Source
well that flange of that intake is on a
gasket so how good is your ground path
really I say it sucks and so uh when the
boat goes back together I don't know if
it'll have nitrous on it or not but it
damn sure won't be grounded to the
intake manifold like that not into it
yeah see there's the bolt that just came
out of there with stuff all over the
threads the other thing I want you guys
to pay attention to is you can see how
oblong the ring terminal
is it's going to fail at some point
because what happens is the washer the
bolt head or you know maybe maybe prior
to this install it didn't have a washer
on it but the bolt head grabs it tries
to spin the ring terminal and then
Oblongs it and you do that enough times
and eventually the ring terminal fails
this is sketchy cuz it's such a thin
plate I don't I don't want to bend it
you
know almost like it's hitting a wall in
there definitely got all the bullets
right
yes
okay there we go just shifted Beauty yay
intake is off let's give the complete
history of this motor as I understand it
guy named Jim guthy built this motor it
was raced by joola Camp successfully as
far as I understand he won a
championship with it I'm not exactly
sure what happened but it broke at some
point dropped a valve I think when I
bought it it was fresh that's what it
was advertised as and I didn't know it
had been wounded I just heard it was
Fresh So after the fact I found out it
had broke and one of the heads had to
get fixed I think by Joey gross of gross
Racing Engines who's fantastic engine
builder so we get it it's fresh go to
the first race it's just got problems
from sitting around you know wiring is
not happy the data system's not happy
there's a bunch of corroded stuff hoses
were junk and it broke some valve
springs and it Milkshake the oil the
very first race I ever went to and so
after that it went back to the engine
builder Mike Miller it was not the
original engine builder but he was he he
had he had refreshed this thing and it
was at that point he was like when I
refreshed it I never changed the Val
Springs cuz they were new so when I took
it back to him it got new valve springs
so seemingly our valve train issues
should have been solved except they
weren't after that we had problems with
it's still milkshaking it's self which
ultimately we figured out at one of the
races it was a paracity problem in the
cylinder head over over there we had a
rocker arm just break had an adjuster to
shove right through the back of the
rocker arm and well when we started
diagnosing why that happened it was
because the rocker stand was loose like
all right well that's weird so we check
them all tighten them all up fig that
problem's gone and then after that it
was just stupid stuff you know we we
decided to go to World Finals and we
decided we didn't have enough in the bag
to be competitive in any of the classes
at World Finals not the 6C bracket class
not the heads up Eight Mile class none
of them so you know we said to Mike can
we go through this thing and put pistons
in it and Rings cuz we know we're not
going to be able to spray any nitrous
into this motor it's got lightweight
Parts in it and he says yeah and it this
was like in August World Finals were in
November and right before World Finals
when he goes to put it together he
realizes that the new Pistons the skirt
hit the counterweights of the crank and
it was like oh crap at that point it
became a mad thrash to hurry up and find
a crank for this because you can't get
Pistons quickly so he finds a crank gets
it balanced a lot of people helped with
transporting it and machining it and all
this stuff it goes together and then it
goes on the dyno at West Tech
performance and I get a phone call from
Steve brle who's running the dyno and
he's frantic he's like the motor's
running hot and The Rocker stands keep
coming coming loose like one by one
they're coming loose the end results of
the dyno test was the motor was down on
power but everybody agreed it was
probably fine let's go race it and we
went and raced it and it lasted like six
passes I think I think at the time I
thought five but it was six basically it
didn't make any power it didn't go fast
and it dropped a valve but now today
we're ripping it apart to figure out why
the motor the entire time I've owned it
has always had something wrong with it
and so I would love to either just fix
it and sell it or fix it and be sure
nothing's wrong with it and we'll put it
in something I just don't know what I
don't know if it's going to go back into
the boat I I'll be honest with you this
motor took the fun out of drag booat
racing real fast for me in the beginning
it was very fun I I let the problems go
I was like whatever it is the boat sat
around fine whatever I'm here with my
friends we're having fun the first few
races were really fun and we won a
couple of races in this boat we kicked
butt which was fun while having problems
with this motor we were winning and in
the end we you know Joe and I were
really looking forward to going to World
Finals we hadn't been in like 15 or 20
years we were fired up about it and that
deal was fun because of who we were with
and where we were at the
racing you know by the time we left we
went you know what we're just going to
take matters in our own hands we're not
going to show up anymore hope things are
right according to I think Mike Miller
it got new valves because I think before
before I got it you know before I bought
it m and the reason the motor was out of
the boat was I think it had dropped a
valve and hurt the head so I believe the
head got repaired and the valves got
replaced but the old Springs got put
back on because they only had a couple
Laps on them and those were the springs
that we were breaking when I bought the
boat so these valves were new but now
that I found out that on the dyno all
the Rockers came loose and The Rocker
stands came loose dude there's no way
I'm going to run these valves again cuz
look what look what just happened you
know we broke one now is the lifter
you're stuck no that's good news so this
is the side that we had a problem
with and this is the side that basically
push rod tip broke off it happened
somewhere between pretty much the launch
ramp and the pit cuz I drove the boat in
and it sounded just fine I made I made
my pass it wasn't fast I drove the boat
put it on the trailer everything was
fine went to the pits started looking at
the data and we're like it's just slow
it's unbelievably slow and I started
questioning the motor and so we go to do
a compression check and we get to number
three and it has zero compression pull
the valve cover off that's when we see
the push rods broke in half go to roll
the motor over and it locks up and
because the head of the valve broke off
so if you look through the number three
exhaust port and I'll give you some
light here Joe so you can show them that
if you look in
here the head of the
valve is sideways it should not be there
you should see the back side of the
valve you shouldn't be seeing the face
of the valve maximum air flow right
there yes and if you look at the guide
there's a chunk of the guide missing
right yeah well if you come over here
this one's doing the same there's a
chunk of that guide missing let's go
look at the other
ones um that one seems okay how about
that one that one looks all right let's
go to the other side because I'm
starting to
wonder did it Bend valves when it was on
the dyo looks all right looks all right
all right so at a minimum we've got one
over there where the guide is broke so
look at this right here right see the
chunk out of the side of this yeah this
is probably one one of the ones that
came loose on the dyno it beat the snot
out of the rocker arm it broke the guide
the valves probably bent and that's why
this thing wasn't making the power it
should have made on the dyno I think I
think the motor was wounded before we
ever ran it at uh World Finals which
sucks but what do you you going to do
well let's take it all apart that's
racing is it
really it I don't know I don't know but
we're going to make the best of we're
going to fix this we're going to make it
right I don't know I feel like we should
fix it and make it better than it was
and put it back in the boat and run it
if that becomes not fun this is a great
motor if we can get rid of the valve
train issues yeah it really is maybe
Pete can get rid of the valve train
issues the big thing for me is do these
heads even go back on because they need
rockers they need valves I don't know
we've had nothing but problems with this
valve train do we even put these back on
good news is it didn't didn't stick the
lifter in the bushing so that's great
news the thing I wonder about is this is
the one that failed how many other bent
valves do we have from when those rocker
stands came loose on the dyno that's
kind of what I want to find out today
and for those of you are at home that
know the history of this motor there's
the part where the head got welded by
Andy RWS after I bought it it was
leaking we tried to fix it with what we
use JB Weld in fact the JB Weld top
secer JB Weld topset JB Weld got us
through two races that we won and then
finally it just started leaking again so
Mike Miller pulled the head off Andy
rolls welded it put it back in service
hasn't leaked since in fact the oil
looks great next thing to do is we will
we can't roll the motor over so have to
be careful when we do this but we'll
take all the Rockers off take all the
push rods out put them in that organizer
and then we'll pull the heads off and
see how screwed up this head is from
where the valve broke off cuz I'm pretty
sure the chamber is going to be beat up
the seat might be broke and then I want
to disassemble both heads to see do we
have any other bent Valves and if we do
we'll go see Pete and then I don't know
does it go back in the boat the Sunny's
motor is already sitting in the boat you
know it just needs headers it just needs
headers and and new computer system or
just a carburetor true like if you put
EFI on it yeah that's a big process but
if you just throw a dominator on it it
has a front drive distributor like this
motor it's sitting in a box we could run
it na that might be the quickest way
back on the water cuz who knows how long
it'll take to fix this thing if you're
ever wondering whether your lifters are
on the base circle of the cam which is
when you want to check for valve lash
when you want to test your Springs if
you have the intake off it's super easy
you can see it so like this one is open
cuz it's up this one is closed cuz it's
down these ones obviously aren't on
anything right now but you can see
that's the base circle of the cam if you
look over here here we'll come to this
one this one is on the base circle of
the cam cuz it's down this one is on the
lobe cuz it's up and if you come up to
the cylinder head side so that's open
the valve you look here The Rocker is
down the valve is open you look at this
one it has lash you can lift it up and
down and if you come down and follow it
that's down it's on the base circle of
the cam and if you look that's the base
circle of the camam there there the one
next to it that I said was open you can
see it's it's on a lobe the lobe is up
and if the intake is on the easiest way
to do this is you just look at the
rocker arms and you can tell whether
it's open or closed um I like to use the
EO I meth method which is if the exhaust
is opening like as soon as it starts to
open then you know the intake is on the
base circle like a big block Chevy and
you can check that one and then IC
intake closing intake opens all the way
up it's closing once you get about
halfway the intake is closing the
exhaust will be on the base Circle
you'll feel lash in it you can check
that one time to pull the head bolts and
then the heads on uh aftermarket big
block
Chevys a lot of
them will have bosses in the valley that
you can put another set of head bolts in
these D big Chiefs have the provisions
for these so instead of the bolt going
into the block this comes up from the
Block into the head this side's
threaded and I don't remember off top of
my head what the torque spec is for
these but these were not amazingly tight
I just grabbed it with my allen wrench
and undid it pretty
easily I I don't remember if it's a 38
or a 7/16 bolt I to look it up when we
put it back together what it's supposed
to
be but long story short you got to get
these four
out then pull the head bolts off then
the heads come
off that one there yeah and then uh and
I don't know why but we have different
Hardware over here this is a socket head
Allen and
then this
is what's
that I don't know what that is a smaller
socket head I don't know why we got two
different sets of Hardware in here it's
weird crap out of that piston not as bad
as I thought it was going to be though
bad not
what is that what's on that one is that
a ding too kind of looks like it looks
like something went in there it's too
bad we didn't have a spare piston for
this motor so far it looks
like the cylinder's okay but yeah it
looks like something hit that one too
it's got a couple of little dents right
there yeah and something right there
it's possible a piece from that one W up
over there went back through the intake
but unlikely but Poss
there's this chunk a little bit of
shrapnel floating around in the lifter
Valley there let's go look at the head
see the head got
[Music]
trashed oh yeah yeah valve seats junk
it's into the heads probably going have
to be welded too that's a bomber those
are big intakes yeah those look like
2450s or maybe even bigger going to go
have to see Pete probably take both
heads and all the valves fix these and
either put it back together or fix these
and sell these and try something
different what are you thinking I don't
know edel Brock has symmetrical Port
deal that supposedly avoids some of the
issues you have with a spread Port deal
offset cup lifters and rocker arms and
right you know you have like when you
put one of these together you end up
with if you look at some of these intake
ports
you end up with some of the hardware
going into the intake PS see right there
that's where that's where a headbolt
breaks into the intake Port you have to
seal the headbolt when you install it
and I believe some of these
issues aren't present with a symetrical
port head but I don't know I've never
used one before the spread Port stuff
flows good it's just it's older
technology like this is all based on Pro
Stock stuff from 30 years ago that's
been changed you know valve angles have
changed
it's a nice set of heads these are dark
big chees allegedly poured by Curtis
bugs they they made great power but we
have not had the reliability with them
so horsepower is awesome but not if it's
temporary yeah they've been a major pain
in our butt yep I don't believe this is
related at all to the cylinder head I
think this was somebody blew it series
of events The Rocker st came loose and
then the push rods fatigued and next
thing you know you have that you know
the question is if we repair this and
make sure the rocker stands are tight
and get the valve Springs right do we
make great power and it lasts or do we
just keep finding new problems there's
the cutter marks where it swiped across
the deck and decked it and that's one of
the roughest decks I've ever seen for an
MLs gasket and maybe that's why the
coating is sprayed on it is maybe that's
the only way to get it to seal but I
don't know most Motors I've ever seen
use an MLs gaset the deck is very very
smooth this is weird and it's worse on
this end than that is this end this end
is much smoother this the first Rod cap
we took out I don't see any signs of
detonation I see you know some trash
went through the coating that's the
streaks but there's no pits there's no
the bearing doesn't look deformed for as
much as we struggled spraying nitrous on
this thing and not going fast we didn't
rattle at least this first piston did
not get rattled that's good
news and it felt like it felt like the
Rings sprung
apart all right so again I don't have
any paperwork on the motor and so I
don't know what the ring gaps were like
originally but if you look the top Ring
The Gap is much smaller than the second
one it doesn't feel like it has a ton of
tension it's possible these are low
tension Rings or it's possible this one
got hot I don't know we'll pull the rest
of them out and see what they look like
and then we can always put the ring in
the boore and measure the gap of what it
is when it's in the boore this side of
the bearing that's interesting
I think the bearings recoded but if you
look it looks like it's starting
something scratched it something went
through it into the next layer of metal
I don't know what the second layer of
metal is in there but see how it's like
kind of a gold color yeah that's
interesting okay looks okay though let's
look at the next one there yeah same
thing this bearing if you look at the
very edge of the bearing yeah you can
see a little bit of the
gold
yeah check the clear is for
sure how's that look same thing it's
down into I don't know if that's copper
or what it is but it's down into that as
far as our ring gaps there's the top one
second one ought to be on the opposite
side and it is the second one's much
bigger now there are there are engine
builders that run the second ring bigger
than the top ring as far as the Gap
again I don't any paperwork I don't know
what this was set to we could call Mike
and ask him cuz I don't know
that bearing stayed in the
rod oh that's
interesting so this is the one we had a
problem with right there's the dent the
top ring Gap is right there the number
two ring in gap should be about 180°
away from it yeah it's right there the
reason you separate them by 180° is so
whatever gases get through this Gap
don't just easily find their way through
the second one so did that one somehow
rotate that one looks okay about the
same so this one's way over here yeah so
there's the top ring 180° out is the
second ring these are scuffed pretty
good for a a brand new motor but maybe
that's I mean it's a tall deck block but
maybe that's indicative of a giant
stroke side loading the 632s they they
they do complain about the side loadad
into the cylinder wall got to be it
right I don't know it's my first one
that's what we'll tell everybody it's my
story I'm sticking to it man you don't
even know you don't know about SI 454
guys you don't even know what's up I
know you can have your chop how's your
side load
yeah got chop I got side load I'll be
wearing out piston skirts every three
seasons yeah
that they don't have that on the edge
one of them didn't but I'm just sitting
here wondering these journals all got
tapered in them or without the nitrous
this thing was down 500
RPM from where oh wow that doesn't want
to come out is it rocked in there
[Music]
somehow you got I'm going to tap it tap
this side over here you got the ring out
on one side not the other okay you
catching it
yep
okay's coming with it okay got it oh
this one's more unhappy than the other
ones it's really copper looking here and
then it looks kind of like Heat going
that direction or it's wearing this way
where is our ring gaps on this one I
didn't look did you see them 180 wow so
so far it's this
one that one looks better except for
this monster scratch right there I
thought it was like a hair but it's not
catch your fingernail on that oh that is
weird weird it's like a it's a scratch
going this direction and you can catch
your fingernail on it huh what is
that these were coated bearings you can
see it at the Pary line but it took the
coating off of these things that didn't
last very
long second one is
there top one is
here far enough not 180 this looks like
a DLC coated wrist
pin two more
see it's darker here and it gets lighter
lighter lighter it didn't get into the
copper but we should measure these
journals feel like they're tapered for
that all that coating to be gone already
it's like a bunch of trash went through
the motor like it was something was
wearing or it was dirty when it went
together one or the
other number seven all right second ring
is here top ring
is here like 45° part that's weird all
right second ring
there top ring
wow it's
weird this is like 45° apart on this
one but
like this so were like almost 180 this
one's about 180 which is where I would
do it this one's
180 this one's like 45
45
45 this was less than 45 now timing
cover needs to come off Main Cap's off
crank out at that point we're done all
right cam shaft coming out I have no
idea what cam this is but it's got to
have a ton of duration and lift to
support you know 11 1200 is naturally
aspirated horsepower hopefully there's
some numbers on it that we can decipher
and call someone to find out cuz I'm
going to guess this has probably
295 270 degrees of duration um but as
far as how much valve lift it's a NY all
right they make good cams and we have
all the numbers we need off of this yeah
we can call isy give them all these
numbers they can tell us what we have
for a cam all right now that the Cam's
out uh we can pull the main caps off
pull the crank out and then we can start
comparing the old parts to the new
parts all right Joe broke loose all the
nut nuts for the main caps and now we're
looking at the main bearings definitely
had trash go through it yeah nothing too
severe but it's definitely had some
trash this is all brand new so yeah
these have I don't know whatever half
hour of dinno time and six laps on them
you can see the scratches in it there's
a pretty good one right there but this
is from debris going through the oil
system and most new engines after you
build them you'll have debris in the oil
system from parts betting in or if you
just didn't do a good job of cleaning
the parts or having a clean environment
when you build the engine it's part of
the reason we swept this place out is
any dirt that ends up inside the engine
goes into the oil and then gets sent
through the oil system and you got to
remember the gap between that bearing
and that
journal let's just say most Racing
Engines like a big block Chevy that
people build it's somewhere around 3,000
of an inch so you're
talking Micron siiz particles Scrat
scratching the coating off the bearing
this wasn't going to fail or anything
it's just you know like you said you can
see that trash went through it I didn't
see any signs of detonation on that
though so that's good news I didn't see
any if nothing else we didn't go fast
but we didn't detonate the motor either
right that's good news it's wild this
engine turned the exact same RPM with
nitrous that it turned when it was
naturally aspirated before personally I
think you know we had a
really really
really fat nitrous tuneup
could be why it was shooting ducks yeah
the the other thing that's interesting
is is I was talking to Josh Patridge
who's good friends with the original
engine builder of this engine and the
guy that used to own the boat Joe the
camp and he told me that uh this thing
was turning 73 7400 RPM and the boat was
running 560s 550s yeah before I got it
never ran that close we've never turned
more than 7,000 when it was naturally
aspirated so it was definitely down on
power like when I bought it from where
it was according to Josh I just talks to
him that's not the cam that was in this
motor originally yeah and looking too
looks like one and two when I unwrap
these old rods the Pistons are marked
but the rods aren't marked like all the
other ones so I'm wondering if the rods
Rod get replaced yeah maybe those two
did did it break a rod or did it break
you know a lifter and or drop a valve
and it ended up I bet what happened what
I understand about this motor is it was
originally built made over, 1300
horsepower won a championship ran for a
season or two it dropped a valve which
is probably why a piston and Rod got
changed or two of them it's probably why
they're not marked and then when it got
refreshed I'm guessing the cam got
changed and it's never made the power it
made before since yeah so it might be
worth looking into if we can find it out
what were the old cam specs lamp ran
lamp ran this thing and won and I don't
I've never heard of him having the
problems we've been having with this
thing you know maybe we go back to some
of the old combination and it makes more
power and lives longer if we even use it
that Sunny's motor is already in the
boat I say we run it and at some point
this goes back together and then the
question is do we run it na a or do we
run it on the bottle if we could rebuild
it and make over 1300 na this thing
would run pretty hard you know even
without nitrous I mean it ran hard when
it was na when we erased it it ran hard
we ran 131 132 mph so we'll get this out
compared to the the old crank we have
the old Pistons we have the old rods we
have the old Crank that came out of this
motor which was not broken we can
eyeball those parts compare them to what
we have and maybe we replace the cam and
the valve train and just put the old
bottom end back in it and see what she
does so now this one looks like it's
been detonated see that right there it
smashed something as it was going
through it oh yeah and this one is
really unhappy Jesus it's down into the
other layer there it wiped the coating
out unevenly wow okay this thing's not
happy that looks like a good crank
though I don't know why it would be
flexing oh
Jesus and that one's really bad too wow
it's wiped this half of the bearing it's
got deep scratches in it wow either the
cranks flexing or there's taper in the
journal or tap taper in the lion hone or
the clearances weren't happy now I'm
really glad we're taking this apart if
we were at the track and we found a
valve and replaced it and just kept
going and spraying it that would have
been bad and the reason I say it would
be bad is cuz unlike a car in a jet boat
if something goes wrong and the motor
locks up you can't just push the clutch
in and pull to the side you can't just
step on the brakes you don't have any of
that in the boat if the motor locks up
the jet drive stops spinning all the
water that's coming into the jet drive
from under the boat has nowhere to go
and basically front of the boat comes
smashing down into the water and you get
thrown out of the boat and it's not good
what I would like to do is if you go
back to this is the number four for main
bearing I would like to measure the
journal on that left to right and see if
there's taper in it cuz if you look at
this that looks brand new right there
and it's all scratched over here that's
brand new that's brand new it's all worn
here and this is worn then this is the
same on this side this one's worn here
here so either the line hone is messed
up or the journal has taper in it or the
crank is really flexing which we're not
making tons of power I'd be surprised if
this crank was flexing like that we
weren't even spraying it hard oh the
journals are scratched up in this thing
wow yeah look at the difference between
these two cranks uh on your right this
is the crank that just came out of our
632 on your left is the crank that came
out of this motor last fall when it was
rebuilt for
nitrous and what I was told by the
engine builder was that the counter
weights on this crank were so large that
the Pistons and rods he ordered from CP
cillo wouldn't fit because the skirt of
the Piston was actually contacting the
counterweight of the crank so here's a
quick comparison of our old piston old
crank new piston new crank now if you
look they are wildly different parts
um this has the the new piston has a
longer skirt so you can see why that was
going to be an issue it has a thicker
area up here the compression height is
taller the Rod is beefier you can look
at this Rod it is very light compared to
this one thicker wall wrist pin larger
wrist pin everything about this says
nitrous you know beat the snot out of
this this is lightweight na horsepower
type Parts really lightweight stuff and
then when you come over to our cranks
I'm not sure but I think this is a sunny
Bryant crank shaft um you can't really
tell because it got balanced where the
name was I believe this one here is a
Callie's the thing that I'm bothered
about this Callie's crank is that it
looks like it never got polished if you
look at all these journals especially
the mains sure they trash went through
them for sure but if you look at the
journals on the old crank this crank has
been run for years we ran it for an
entire season and it's beautiful this I
I'm questioning whether once it was
sized all these journals did it ever get
polished I I don't even know but yeah
it's interesting but we definitely when
you move over here we definitely have a
problem with either the crank flexing
and trying to take out the number uh
three and four main bearings or there's
taper in these journals or the line hone
in the block is off I don't know when
when you start looking at this old crank
like I'm going to compare this one here
to this one that wear is pretty even
from here to here yeah it looks really
good to my eyeball whereas this wear
looks brand new on this side and wore
out on this side which is what you see
on the bearing the only thing we can do
here at my house in my garage is we can
grab a micrometer and measure these
journals in a couple places and see if
we can find taper there we could pull
the bearings out of the block and torque
the Caps back on and we could check the
line hone um at least journal to journal
I can do that with a dial board gauge
short of that there's not much I can do
here with my knowledge base remember I'm
not a professional engine builder nor am
I a machinist I don't have any tools to
repair this stuff so I'm I'm an engine
assembler I can do that I've done that
pretty successfully in the past we can
build this engine once the machine work
is you know happy and the parts are
happy so I think our next step will be
we'll put the crank up on the bench grab
the mics measure it and see if there's
taper in it um if there's not taper in
it I'll assume guessing that number one
exhaust valve has an issue since the
guide is busted those are probably the
last few things we do with this and then
at that you know it's just okay look at
all the parts we got some point we'll
put it all back
together just not today Satan not
today
all right everybody at home this is an
outside micrometer this is what I used
to measure the
crankshaft I've got it set up in a pair
of soft Jaws lightly clamped in my Vise
so as not to twist this thing as best I
can keep in mind I am not a machinist
but I learned a few things like how to
read this thing this is the thimble this
is the sleeve this line right here is
the line that we use to read the numbers
and we start down here with zero so if
we thread this all the way in to zero we
are lined up right there now as I open
the jaw and we move this one 2 3 four
five 6 7 8 9 10 15
20 when I get back to zero I've exposed
the first line that's 25,000 of an inch
if I keep going we're at
45,000 zero again there's two lines
showing
50,000
75,000 100,000 then you're going to see
the number one appear right there so
essentially what's in the Jaws right now
is 100,000 of an inch thick now if you
keep going we'll just we'll just pick a
a random number over here a random thing
to measure this thing is is 200,000 of
an inch plus
2550 plus three we're not quite to four
so we're
253,000 not quite four so then we got to
move over here and what we do is we look
right here on the sleeve until we get a
line here that perfectly lines up over
here and in this case we're at
253,000
plus 4 so if you were to write that on
piece of paper it would be decimal
2534 and that's essentially how you read
this thing and this is the tool we used
to measure the main journals on our
crankshaft and figure out there was no
taper there that's not why our bearings
got taken out in our engine block it's
the next day I'm dressed differently
obviously today's going to be a good day
cuz we are about to learn a whole lot
together now if you recall yesterday
when we were tearing this motor apart we
didn't have a good reason why the
bearings look the way they did this is
what I'm talking about this is the
number four main bearing this is the
number three main bearing they are just
wiped out and oddly enough it's the
bottom half of the main right this is
the cap bolts onto the block this is the
bottom half this is where a lot of
pressure is present on the crankshaft
pushing down at all times cylinder
pressure but when you detonate something
you have even more and when you
physically have Parts hitting each other
pistons and valves you have even more I
think I'm pretty sure what we have going
on is metalo metal contact between the
exhaust valves and our pistons and I'm
going to show you why let's go through
the sequence of events race the boat
last November right before the race the
motor got rebuilt for nitrous it got a
new crank new rods new pistons on the
dyno which I wasn't there for I just
heard secondhand The Rocker stands were
coming loose on these cylinder heads the
dart big Chiefs and it was chocked up to
them needing Loctite which in hindsight
I've had spread Port style heads before
on engines I've owned I've never had to
locktite The Rocker stands to keep them
tight it's kind of odd yesterday we were
looking at all the bearings and I I
thought maybe the crank had taper and it
measured that the crank did not have
taper I didn't have a good reason for
why the bearings were wearing so I
started calling people I talked to Joey
gross who facilitated the crank getting
machined and ground and Polished he
verified that yeah it's all scratched up
cuz metal went through it but it was
polished I said okay I talked to Steve
Brule I talked to of West Tech
performance and bounc some ideas I had
off of him I talked to Mike Miller the
guy who built the motor Mike's opinion
was the bearings look like the motor had
detonated I thought to myself when we
were racing the whole weekend Mike
myself Joe everyone in our pit was
looking at the spark plugs constantly
because the boat just kept getting
slower at no point did I ever see any
sign on those spark plugs of the motor
detonating we would have seen aluminum
particles on the porcelain of the Piston
we didn't see see that we would have
seen peppering you know brown spots from
the fuel on the porcelain we weren't
seeing that nothing about this said this
thing's detonating and yet it was
getting slower almost every pass in
hindsight I wish we had cut the oil
filter open because we probably would
have realized the motor was eating
itself alive and we probably could have
stopped running it before the you know
exhaust valve on number three broke in
half but we didn't it's neither here nor
there so after talking to all these guys
yesterday I came back in the garage last
night and really started staring at the
combustion Chambers in the cylinder
heads and the Pistons I stopped looking
at bearings and started looking for a
cause for why the bearings looked the
way they looked and one of the things I
noticed was and this is the number one
piston out of this motor I started
seeing stuff on the Piston that didn't
make any sense to me on the Piston
there's swirl marks in the valve Rel Lea
for the exhaust valve and I thought to
myself okay that's weird cuz it doesn't
have it on the intake valve relief and
and I thought are those machine marks
well I don't know if it's machined in a
circular pattern there then this relief
would have it as well and it doesn't so
then I went to the cylinder head the
intake valve looks brand new you can see
the word manly written right on it and
there's no swirl mark But if you go to
the exhaust valve almost every one of
these there is a perfect machine Circle
in the middle of the exhaust valve that
matches the circle that's in the top of
the piston and the same circular swirl
marks now I got to call Manley real
quick but I'm pretty sure when I do if
they send me a picture of one of their
valves it's going to look a lot like the
intake valve it's going to look smooth
it's not going to look like it has swirl
marks and so once I noticed those two
things I started thinking you know these
valves rotate as they're going up and
down opening and closing I think the
exhaust valve is hitting the piston and
that's why you have the same mark on the
Piston that you do on the valve I took
it a step further
I called my buddy Brian uh at CP pistons
and said I need a picture of the Piston
before you know right after he got
machined before it was installed and
sure enough it looks a lot like it does
now except it doesn't have those swirl
marks in it and I said all right I'm on
to something so then I took bottles of
water and started filling the exhaust
ports and they're leaking the valves are
not seated anymore which tells me
they're probably bent and they're
probably bent because I think while the
engine was running those valves were
touching the Pistons over and over and
over again and they were spinning which
is what put the pattern in there and the
real Telltale here is if you put the
piston this is the number one piston
next to the number one chamber if you
put them next to each
other that pattern looks an awful lot
like that pattern right twinsies right
and I just so happen to have all the
Pistons out of this motor from when it
was naturally aspirated if you put it in
there this is the number one
piston you don't have that there's no
swirl pattern there's no circular mark
this does not match which tells me that
when the crank rods and pistons got
changed in this motor it didn't have
enough piston to valve clearance now
there's something else going on here
every one of these intake valve Pockets
has witness marks on them and the odds
of debris going through the motor and
landing in the intake valve pocket on
every piston and the exact in the exact
same spot is pretty slim so I'm thinking
we might also not have enough piston the
valve clearance on the intake valve I
don't think it's as bad as it was the
exhaust I mean clearly we broke an
exhaust valve in half the intake might
be an issue as well my synopsis here my
reason for why this motor ate itself
alive is that it was never happy after
it got rebuilt we had Pistons kissing
valves at 7,000 RPM but I am going to
learn something here what we're about to
do now is put the crank back in the
motor put the number one piston back in
put the head on with some lightweight
Springs and we're going to measure the
Piston the valve clearance and we're
going to find out with a steel rod and a
titanium valve in this motor how much is
enough cuz whatever we have here is not
enough piston valve clearance and once
we know that info then we know going
forward okay if we ever put this thing
back together we need deeper valve
reliefs in these Pistons or the Pistons
need to be moved down in the boore
something has to change about this
because if you if you just replace all
the same parts that are in it put it
back together it's going to die again
I'm actually surprised it lasted six
laps like this is wild to me what
started this whole thing is I had all
these Pistons sitting on my workbench
and I started staring at them and I'm
like I don't understand why these
bearings are getting wasted and I
noticed I think four or five of these
Pistons have a dent a chunk taken out of
the skirt where it's been hitting
something if you look right
here this surface and then boom right
there you can you can grab your finger
on on it the skirt is dented downwards
and you can catch your finger on it
because this hit something when the
motor got rebuilt for nitrous the plan
was just to put pistons and rods in it
we have a a really nice sunny Bryant
crank in this motor I guess when Mike
went to put it together the new piston
skirts wouldn't clear our crank so we
had to hurry up and overnight a brand
new crank and have it machined and have
it polished and have it sized and then
put it together well they're still
hitting so it adds a little bit of
insult to injury that I bought another
Crank That
you know ultimately didn't work it is
what it is we're going to have to
replace a lot of parts in this motor the
crank's not junk but every valve's got
to get replaced every piston hopefully
the rods are okay the wrist pins are
probably flexed from all the the
pounding they took the end result of all
of this is probably bent valves the
Pistons are compromised all the trash
from all the parts rubbing on each other
went into the oil system and scuffed the
cylinder walls scuffed the skirts of the
Pistons like the crank's going to be all
right the head needs to be repaired the
blocks fine you know the big parts are
going to be okay but but we're going to
have to replace a lot of stuff and I
don't know that I'm even going to do
that anytime soon because the Sunny's
motor which has proven itself to be
really reliable is sitting in side chick
I'm probably just going to make that run
figure this out later but for now we're
going to turn lemons and lemonade we're
going to find out how much piston of
valve clearance is enough for this motor
that was really long I'm
[Music]
sorry main caps are in we are about to
put the nuts and washers these are ARP
half in studs ARP is closed right now
because they're on the west coast and
it's in the morning on the East Coast so
I called Dart to find out what they
recommend for torque spec for this and
they have all their torque specs using
something called CMD number three not
ARP Ultra torque Fastener assembly Lube
but for our purposes we're not going to
run the motor we're just going to torque
the Caps down so the crank is in place
they said 105 we'll do 105 with this and
like I said we're not going to run the
motor it'll be fine so right now I'm
scraping all the silicone off of our
timing Cod cover
because
this needs to be a flat
surface again we're not running the
motor
but this is a jezel timing cover for a
belt
driven there is a spec and it's between
8 and 12,000 of an inch for the end play
or the thrust of the cam as it moves
forward and back in the block and so
there are shims in here that set that
you know ultimately when the motor goes
back together I don't want a bunch of
silicone stacked up when we install this
and since Joe's doing one thing and I'm
doing another I might as well just clean
it while I'm here and it'll be ready for
when we actually put this motor together
and run it at a later date for what
we're doing today just checking piston
the valve
clearance all right right now Joe is
cleaning the cam getting it ready to go
back in the motor I'm going to wipe off
the cam bearings make sure they're okay
and whoa they're not okay these things
are all chewed
up
hello oh yeah I got gouges deep enough
to catch your fingernail on them okay
these are getting changed too we'll Lube
them up it'll be enough for checking
piston about clearance be all
[Applause]
right W that's
close woo it's close and it's not so I'd
say the wristpin support the bottom of
the Piston where the wrist pin slides
through is got a solid eighth of an inch
between the counterweight and that and
when you rotate the Piston right at
bottom dead center you can see where the
skirt nicked a counterweight would have
been that one cuz that was the first
Crank that was in this motor cuz it
never makes you slide this in you start
rotating it it doesn't get around one
full res Revolution so how did the other
four get dented unless there's something
about this crank that's denting the
other ones like maybe number one got
dented with that crank during you know
the assembly process and then whoaa okay
order a new crank order this crank put
this crank in slide all of them in there
and the other ones got dented after the
fact on the second go round there's an
eighth of an inch because of the dent so
if the Dent's not there wait a minute
maybe they're still hitting it's because
of the dent we have the clearance that's
the tightest point right there see that
yeah oh they're hitting the so now find
the one for number five be right here
somewhere so it would be the Inside Edge
bottom dead center right so it would be
right in here so when this when this
rotates around we need to look at that
area let's look at another one got Nick
six not as bad as the others but well
that would explain I mean we're because
these two weights are almost identical
here you know what I mean number six got
it so let's see that' be on this side
this side and it would be valve relief
there number six got hit here which
should be here this counter weight this
one might be hard to see cuz it's a
really light just barely there was
another one that was pretty bad like the
first one yeah here you go number two is
number two is smacked hard you see that
you can feel it right there all right so
it would be on this side relief is there
it would be here so go it would be
somewhere right here so rotate it back
up I think that's it right
there so think got a big lip on it feel
that oh yeah catch your fingernail on it
I think it got it right there I mean we
can we call and ask Mike and be like all
right how many got dented during mockup
all right let's flip it over we'll find
top dead center we'll put the balancer
back on and the degree wheel because
it's aluminum block right now we're
going to figure out how far in or out of
the hole the Piston is in relation to
the deck surface uh we've already done
that once but we're going to double
check it anyway because this is domed we
can't put the dial indicator in the
middle of it so what we're going to do
is we're going to move it to the outside
Mark right here we'll zero it raise it
up a little bit so that it so that it
has some travel we will Zero it on the
deck surface and then we'll place it on
the Piston if you can hold it here I'll
try to find TDC in the hole and now it
is 21 in the hole if I rock it the other
way it is even with the deck surface so
if you cut 21 and a half it's about in
the hole about 10 th which is
interesting cuz earlier we measured it
and it was out of the hole let's go to
the other side here and see if that
works out I'll hold it and you rock it
tell me what you see you're at
zero okay that rocked up what's it now
about out yeah okay now push the other
side and go down 23 in the hole rock it
back the other way about a th out of the
hole so 22 so it's about 11 in the hole
10 or 11 when it's when it's not rocking
it's about 11,000 but this thing is
somewhere around 11 11 and half thousand
in the hole when it's level
now we're at TDC we can put our upper
gear on line up our dots and we haven't
changed anything so this should all go
back together exactly the way it came
off got it on we are on all right the
dots line up
perfect and uh we are at
TDC and we never broke these loose so
the cam timing is exactly the way it was
when we took the motor apart which
according to this was 2°
Advanced all right and that is your TDC
Mark all right now it's time for head
gasket and cylinder head now we're going
to clean the head gasket put the head
gasket on the motor and then we're going
to mock up the cylinder head with a
rocker arm and a push rod and before we
do that we're going to take out these
valve springs now these are the Val
Springs that are actually in the
cylinder head in the motor when it's
running they have a ton of Seat pressure
open pressure we're going to take these
out and put lightweight Springs in
they're called checking Springs that
will allow us to operate the valves
without all that seat pressure and open
pressure the cylinder heads are marked
so we know which side of the motor this
head was on that's number one number
three number five number seven so this
is the one will be working with we'll
show you two different ways you can take
these Springs off right
now we are now going to put the cylinder
heads on and measure our piston to valve
clearance which essentially is the gap
between the face of the intake into the
exhaust valve and the Piston where the
relief area is for each one of those at
various points essentially when the
engine's running and the Piston's coming
up and it starts to come back down the
intake valve is chasing it the closest
point between those two things are about
10° after top dead center the exhaust
Val valve the Piston is chasing it out
basically the valve opens and as the
Piston comes up the valve has to close
quick enough so the Piston doesn't run
into it and so the closest point between
those two things is about 10° before top
dead center now to test this we're going
to remove the springs that are on the
cylinder head these are these monster
pack racing springs they have a ton of
Seat pressure I think about 400 lbs they
have a lot of open pressure probably
about a th I don't have the specs on
them to make this easier to to measure
we're going to remove these real quick
and then we're going to replace them
with these soft Checker Springs and
there's a couple ways to do this I have
two different tools both of them are
from LSM this tool is an onad spring
compressor so essentially you can bolt
this to where the rocker stand used to
go put a wrench on it and compress the
spring I also have this one which is a
little easier to work with when the
cylinder heads are just lying about this
is another spring compressor that you
would operate just like this not bolting
into the head it's got a crank on this
end it's got a knurled part right here
that you can put a uh socket onto and
impact this end if you want same deal
compress the spring get the keeper out
pull the retainer off pull the spring
out replace the
spring okay there we go all right
where's the
magnet I'll just mag I'll just magnet
these off the
floor all right now gently release it
and because these were hitting the
Pistons they're probably bent which
means we can probably try to move the
valve move the valve a bit right now and
it's probably not going to want to do it
too well oh it did oh and it does not
want to come out so I'm not going to put
it in the lathe I'm going to let it go
the way it is all right so there's that
put a checking spring in there and this
we can compress by hand and reassemble
okay Old Spring is out we're getting to
ready to put our checking spring in uh
can you grab a flashlight real quick I
want to show the people at home so this
valve doesn't want to come out it gets
about that far and then I'm tugging on
it it really doesn't want to go you see
that right
there that valve guide used to stick
into the port about an inch and it
doesn't probably because the valve bent
in the guide because it was hitting the
Piston so I'm not going to try to get
that out any further we're just going to
put the spring in it and hopefully have
enough travel which I think we do to uh
measure our piston valve clearance
one down one to
go we
compressed there's the
keeper now we'll release the
handle okay stuck in our inner spring
here that's going to go
there compress it on here there we go
okay there's that
one dude you're the man you're holding
the camera you're holding the valve
all
right Bueno and now we're ready to put
our head back
on
go
this is the exhaust which should come
closest to the Piston at about 10°
before top dead center because basically
what's happening is the the Piston is
coming up pushing the exhaust out as the
valve is open and the valve doesn't
start closing until the Piston gets
pretty close right about 10° for top
dead center going to rotate this and if
you want to watch this in real time you
can look down the bottom and see what
the Piston's doing this valve is opening
so go ahead and for the people at home
call it out tell me what the Piston's
doing while I'm rotating this here the
exhaust valve has opened about 100 th000
uh and it's almost all the way down
200,000
300,000 pists all the way
4,000
500,000 600,000 you should start coming
back up
700,000 Piston's about a quarter the way
up
800,000 that is about Peak valve lift
and piston is on its way up it's the
exhaust valve is now starting to close
and we are about 80 degrees before we
get to top dead center and so if is
almost about 3/4 way up and should be
all the way up exhaust valve is still
shutting we are 10° for top dead center
and the exhaust valve is still closing
so picture that in your heads folks the
Piston is only 10° away in terms of
crankshaft rotation to being at top dead
center our exhaust valve is still
shutting so the Piston is chasing the
valve up this should be the closest
point that the exhaust valve and the
Piston are in terms terms of each one's
travel so now what we're going to do is
we're going to zero our dial indicator
here okay that's zero and we're just
going to activate the rocker arm by hand
and however much this travels is how
much piss the valve clearance we have
I've seen people run Motors as tight as
50,000 of an inch I've had
150 let's go a little
tight
100 35
135 let's try
7°
25 which is quite a
bit I would think that would be
plenty all right 125 thou that sounds
like that ought to be enough but clearly
it's not because everything's touching
we we'll
reverifying the spark plug hole piss the
valve clearance on paper seems okay we
have
125,000 p2v for the exhaust we have 100
on the intake and on paper I feel like
that would be a decent number except you
can't get around the fact that there's
witness marks on every piston in every
pocket for both intake and exhaust so
right now we're going to stick some
valves in the lathe and see are they
bent are there any witness marks on the
valves uh that'll pretty much confirm
what's going on and in the end it might
not be a piss in the valve clearance
necessarily it might be a lack of valve
control where the spring that's in there
installed height spring pressure
whatever might not be correct and the
valves are bouncing when they shut you
know so in the case of the exhaust as
the Piston's coming up and it's chasing
the valve and the valve closes and maybe
bounces off the seat and tags the Piston
I don't know let's see if these things
are bent or not I got a feeling they are
kind of looks like right there here put
them in the lath see if they're bent too
oh yeah we are bent valves hitting
Pistons the end of the story now the
question is oh there's my lovely bride
I'm not even going to tell her what I
spent to build it to go nitrous racing
and we're probably not going to talk
about rebuilding it because I'm not
doing that anytime soon here's the thing
I know that this video does not paint
the engine builder Mike Miller in the
best light but here's what you need to
know about this guy we are still friends
he is a really really great engine
builder he has built engines for record
setting Jet Boats the boat that I came
in second place to in my class this year
powered by one of his engines and he's
driven Jet Boats faster than I probably
ever will I think he had a bad couple of
days at work missed a couple of things
that just needed to get measured and
didn't because he was in a hurry the guy
works two jobs I get it uh we have
talked on the phone more than once he
handled me going behind him and
questioning his work and measuring it
better than most guys would have so I
give him a lot of credit for that uh and
my hope is that you know he and I come
to an agreement and work this out um I'm
sure we will I'm not not going to stress
over that and hopefully he doesn't watch
this YouTube video and you know get real
upset with me about it because I just
want to learn just want to know and I
like working on my own stuff I prefer it
actually the boat has been on the west
coast I lived in Georgia the only way
for me to race it was to leave it on the
west coast and put it in the trusted
hands of my friends and he busted his
butt on numerous occasions to get that
engine and that boat ready to go racing
just missed a few things it happens
anyway thanks for watching Fan's garage
hopefully this was educational I know I
learned a few things here today and uh
it's always good to get your hands dirty
in the garage this motor not going back
inside chick anytime soon Sunny Leonard
motor that's going inside chick and next
week back work on the
[Music]
Cadillac
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