Budaya Kerja Korea Menjadi Tragedi KoreanAir 8509
Summary
TLDRThe video recounts the tragic crash of Korean Air flight 8509, a cargo flight operated by a Boeing 747 in 1999. After a smooth flight from South Korea to Uzbekistan, the aircraft experienced a fatal accident during takeoff from London’s Stansted Airport. Despite multiple warnings, the crew ignored critical issues with the plane’s instruments, leading to a crash shortly after departure. Investigation revealed failures in communication, inadequate technical support, and a hierarchical culture among the crew as contributing factors. The incident led to reforms in flight training at Korean Air and significant changes in aviation safety protocols.
Takeaways
- 😀 A Boeing 747 cargo flight, Korean Air 8509, took off from South Korea on December 22, 1999, without passengers, only crew members on board.
- 😀 The flight was scheduled to stop in Uzbekistan and then proceed to London, with a return route to South Korea, passing through Milan and Uzbekistan.
- 😀 The aircraft had over 83,000 flight hours and had a smooth initial journey to Uzbekistan before continuing to London.
- 😀 The flight crew included a highly experienced captain, a first officer with less experience on the Boeing 747, and a flight engineer with substantial flying hours.
- 😀 Prior to takeoff from Stansted Airport, the crew faced a delay due to missing flight plans, which led to a 1-hour hold before departure.
- 😀 Shortly after takeoff, the aircraft began tilting to the left, and the captain failed to heed warnings from the flight engineer about the dangerous angle.
- 😀 The plane crashed less than two kilometers from the airport, exploding due to a large amount of fuel onboard.
- 😀 Witnesses, including one named Gary, reported hearing the plane in distress before it crashed and exploded in the area near the airport.
- 😀 The investigation revealed a malfunction in the plane's attitude indicator (ID), which the captain ignored during the critical moments of the flight.
- 😀 A critical failure was found in the inertial navigation system (INS), which caused faulty data to be fed into the cockpit instruments, worsening the situation.
- 😀 Investigators discovered that cultural factors and rigid hierarchical relationships in the Korean Air crew contributed to poor decision-making and communication in the cockpit, leading to the crash.
Q & A
What was the main cause of the Korean Air Flight 8509 crash?
-The main cause of the crash was a combination of pilot error and technical malfunctions, particularly the failure of the attitude indicator (ID) in the cockpit, which led to the aircraft being flown in an incorrect position. Additionally, the crew's failure to effectively communicate and address the issue contributed to the disaster.
What was the condition of the aircraft before the crash?
-The aircraft, a Boeing 747, had accumulated over 83,000 flight hours and was considered operational. However, the attitude indicator (ID) in the cockpit malfunctioned, leading to misinterpretation of the aircraft's position during flight.
How did the failure of the attitude indicator affect the flight?
-The malfunction of the attitude indicator caused the pilots to misinterpret the aircraft's orientation. The plane was flying in a left bank, but the instrument appeared normal. This led to the crew being unaware of the excessive bank, which eventually caused the aircraft to crash.
What role did the first officer play during the flight, and how did they respond to the situation?
-The first officer, despite being aware of the abnormal situation and the aircraft's banking, did not intervene or challenge the captain's decisions. This lack of action was influenced by a hierarchical and submissive culture within the airline, as well as the captain's authoritative demeanor.
How did the captain of Flight 8509 react to warnings from the flight engineer?
-The captain ignored the flight engineer's warnings about the aircraft's excessive banking. Despite the engineer's urgent alerts, the captain continued to believe the aircraft was in a normal condition, which ultimately led to the crash.
What did the investigation reveal about the cockpit communication dynamics?
-The investigation revealed that the cockpit communication was severely impaired by a rigid hierarchical culture, where the captain's authority went unquestioned. The first officer did not speak up or take control, even when it was clear the aircraft was in danger.
What did the investigation find about the role of the technician who worked on the aircraft before departure?
-The technician who worked on the malfunctioning attitude indicator did not properly diagnose or repair the issue. He lacked the necessary tools and expertise, and the fix he attempted was ultimately ineffective. The problem was not identified correctly, which contributed to the subsequent flight failure.
How did the crew's actions contribute to the failure to recover the aircraft?
-The crew's failure to communicate effectively, particularly the captain's dismissal of warnings and the first officer's passive behavior, prevented the crew from correcting the aircraft's position. This lack of teamwork and decisive action led to the aircraft's continued descent and eventual crash.
What were the outcomes of the investigation into Flight 8509?
-The investigation concluded that the crash was caused by a combination of technical failure, crew errors, and the failure to properly address the malfunction of the aircraft's instruments. The investigation also highlighted the negative effects of Korean Air's rigid hierarchical structure, which inhibited effective communication and decision-making in the cockpit.
How did Korean Air respond to the crash and its aftermath?
-After the crash, Korean Air took steps to improve its training programs, especially regarding cockpit communication and the roles of crew members. They worked to rebuild their reputation, and the airline is now considered one of the respected carriers in the world.
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